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刘小康, 杨圣文, 蒋传文. 硬盘磁头焊点优化及可靠性分析[J]. 焊接学报, 2006, (8): 83-87.
引用本文: 刘小康, 杨圣文, 蒋传文. 硬盘磁头焊点优化及可靠性分析[J]. 焊接学报, 2006, (8): 83-87.
LIU Xiaokang, YANG Shengwen, JANG Chuanwen. Joint optimization and its reliability analysis of hand disk magnetic head[J]. TRANSACTIONS OF THE CHINA WELDING INSTITUTION, 2006, (8): 83-87.
Citation: LIU Xiaokang, YANG Shengwen, JANG Chuanwen. Joint optimization and its reliability analysis of hand disk magnetic head[J]. TRANSACTIONS OF THE CHINA WELDING INSTITUTION, 2006, (8): 83-87.

硬盘磁头焊点优化及可靠性分析

Joint optimization and its reliability analysis of hand disk magnetic head

  • 摘要: 研究了导致硬盘磁头焊点缺陷的主要原因,将焊点缺陷分为两类,并有针对性地提出了优化方案。针对第一类缺陷,建立了锡球势能模型和能量控制方程,通过Sur-faceEvolver软件模拟优化了锡球大小和焊盘之间的相对位置对焊点成形的影响,得到锡球大尺寸为120μ m±5μ m,焊盘相对位置DM-SDS-M分别为2.5~5.0μ m和20~40μ m。针对第二类缺陷,优化了磁头焊盘金属层结构、厚度和悬挂线焊盘引出线宽度,金属层厚度由5μ m减为2~3μ m,同时将悬挂线焊盘引线宽度变小。结果表明,金属间化合物减少了,同时避免了因悬挂线散热过快而出现金属间化合物沉降分层的现象;优化后的焊点经700次循环测试,缺陷出现率由7%~8%减为0.63%。

     

    Abstract: The soldered joint flaws were studied and the optimum solutions were given on the base of classifying the flaws into two kinds.For the first flaw, the energy control equation was established to stimulate the effect of ball size and the relative position to the formation of soldered joint using the Surface Evolver software.The result shows that the optimum ball size is 120μm ±5μm, and length of the slidered pad to the suspension pad DM-S is 2.5~5.0μm, the distance of the suspension pad to the slidered pad DS-M is 20~40μm. For the second flaw, the Au layer is optimized from 5μm to 2~3μm and the leading wire was shorten to avoid the formation of intermetallics deposit flaws.The optimum result shows that the soldered joint undergo 700 circle test circulate, the percent of flaws in the solder joint was shorten from 7%~8% to 0.63%.

     

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